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Aviation AO-2002-005

On Tuesday 30 April 2002, at about 1630, New Zealand Helicopters Hughes 369D helicopter ZK-HRV was being flown on a scenic passenger flight from Mount Tarawera to the company base near Rotorua when engine trouble arose. Before the pilot could land the helicopter, the engine failed and he was forced to make an auto-rotational landing on difficult terrain, where the helicopter rolled over. None of the 4 occupants was injured in the accident. The engine failed from oil starvation, following a fracture of a fitting in the oil line to the torque gauge.

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Rail RO-2002-111

[A preliminary investigation showed that the circumstances were not likely to have significant implications for transport safety. Consistent with section 13 of the TAIC Act the Commission discontinued the investigation and no report was published.]

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Aviation AO-2002-004

On Wednesday 10 April 2002 at about 1435, Cessna 210N Centurion ZK-TWA departed from Dunedin bound for Masterton. The aircraft did not arrive at Masterton, but was not reported overdue until the next day. After a search the aircraft was found on the Friday morning near Conical Peak, 34 km southwest of Oamaru. The aircraft was destroyed and the pilot did not survive. The aircraft had struck the side of a ridge in an upright attitude, having descended as it approached the ridge, due either to pilot inattention or incapacitation.

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Rail RO-2002-110

On Friday 5 April 2002 at about 0806, the locomotives for the Tranz Alpine passenger express collided with the stationary passenger car consist, which had been placed to the Christchurch station platform in preparation for the locomotives to be attached. The locomotive engineer, who was driving from the lead locomotive, was not injured and major damage was confined to 2 passenger cars. The consist was unoccupied at the time. The safety issue identified was an incorrect component fitted to the locomotive braking system.

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Aviation AO-2002-003

On Friday 15 March 2002, at about 0945, ZK-HIC, a Schweizer 269C helicopter, lost tail rotor authority during a low-level spraying run. Normal helicopter control was lost and the pilot, unable to arrest the ensuing spin, carried out an emergency landing. The pilot, the only occupant, was uninjured. A defective tail rotor driveshaft aft bumper plug permitted the driveshaft to disengage its drive coupling to the tail rotor gearbox.

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Maritime MO-2002-203

On Friday 1 March 2002 at about 1130, while assisting a tanker to depart from the Lyttelton oil wharf, the master of the harbour tug "Purau" lost control and the tug’s stern grounded, causing damage to the starboard propeller and drive shaft. The safety issues identified included: • poor ergonomics of the propulsion controls on the 2 port company tugs • incomplete training of staff • imbalance of the calibration of the propulsion units • unauthorised persons on board the tug Safety recommendations were made to Lyttelton Port Company to address the safety issues.

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Maritime MO-2002-202

[A preliminary investigation showed that the circumstances were not likely to have significant implications for transport safety. Consistent with section 13 of the TAIC Act the Commission discontinued the investigation and no report was published.]

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Rail RO-2002-109

[A preliminary investigation showed that the circumstances were not likely to have significant implications for transport safety. Consistent with section 13 of the TAIC Act the Commission discontinued the investigation and no report was published.]

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Maritime MO-2002-201

On Wednesday 6 February 2002, at about 2152, the log carrier "Jody F Millennium" with a master and 18 crew on board, grounded in the Gisborne approach channel when it encountered large swells as it left the relative shelter of the breakwater while departing from the port. The ship was subsequently driven by the swell on to the shelving shoal area to the north of the channel, where it remained for 18 days before being re-floated. At the time of the grounding the ship was still within the pilotage area, but the pilot had disembarked a few minutes earlier.

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Rail RO-2002-108

[A preliminary investigation showed that the circumstances were not likely to have significant implications for transport safety. Consistent with section 13 of the TAIC Act the Commission discontinued the investigation and no report was published.]

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Rail RO-2002-107

On Tuesday 29 January 2002 at about 1119, express freight Train 530 collided with a stationary shunting locomotive in New Plymouth when the locomotive engineer fell asleep briefly while berthing. There were no injuries and the locomotives were only slightly damaged. The following safety issues were identified: • the restorative sleep habits of the locomotive engineer while working night shifts • the inability of the locomotive vigilance system to overcome short-term attention deficits in time to prevent this type of accident.

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Rail RO-2002-106

This report examines 3 separate track buckle occurrences on the South Island coal route during the summer of 2001/2002. Two of the track buckles resulted in derailments. Safety issues identified by these incidents included: • the need for staff training to ensure they recognise and respond to visible track defects • the need to protect continuous welded rail, formed at unknown neutral temperature • the need to control tamping and lining to ensure track is not realigned leaving increased compressive stress in the rails.

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