On Friday 7 January 2005, at 1852, ZK-KFB, a Gulfstream G-IV, and ZK-FTR, a Piper PA 28, came into close proximity 10 nautical miles south of Taupo Aerodrome, during their instrument approaches to the aerodrome. On board ZK-KFB were 5 passengers, a flight attendant and 2 pilots. On board ZK-FTR were a passenger and the pilot.
Incident date: Publish date:The skipper of the "Doctor Hook" made a distress call. Some of the passengers on board the "Doctor Hook" were initially transferred to the "Quickcat" for medical care and then to a Police boat. The others and the skipper were treated on board the "Doctor Hook," transferring to a Coastguard boat before they were all transported ashore for hospital treatment.
Incident date: Publish date:On Wednesday 22 December 2004, ZK-HHT, a Hughes 369D helicopter was carrying a party of 3 kayakers into the upper reaches of Wanganui River, South Westland. The party’s kayaks and paddles were suspended in a cargo net underneath the helicopter. As the helicopter flew up the river the net swung back and struck the tail rotor, resulting in an immediate loss of tail rotor control.
Incident date: Publish date:On Saturday 18 December 2004, at about 1510 the restricted limit passenger vessel "Tiger III," while on a cruise to the Hole in the Rock with 59 passengers and 3 crew on board, grounded in the small bay under the Cape Brett lighthouse. The boat was pushed into a narrow gut and came to rest alongside the rocks on the shore. All the passengers were able to get ashore and congregated at the old lighthouse keeper’s cottage, from where they were flown by a fleet of helicopters back to Paihia. No major injuries were sustained.
Incident date: Publish date:On Wednesday 15 December 2004 at about 1450, ZK-JES, a Cessna 172, on a flight from Kerikeri to Waitiki Airstrip, ditched in Cable Bay when the pilot could no longer continue flying visually, because of the weather conditions. One of the 2 passengers drowned, and the other passenger and the pilot were seriously injured.
Incident date: Publish date:On Saturday 4 December 2004, a Tranz Metro electric multiple unit passenger train travelling from Wellington to Paraparaumu became disabled between Kaiwharawhara Station and Tunnel 1 when the traction overhead contact wire failed due to tensile overload. The failure was brought about by a combination of poor eletrical contact between the contact wire and stirrup clamping plates, and a build-up of corrosion products.
Incident date: Publish date:On Tuesday 30 November 2004, ZK-JAN, a Piper PA34-200T Seneca II, was on an air transport charter flight returning to Nelson from New Plymouth with the pilot and one passenger on board. After departing New Plymouth and obtaining approval to operate up to 8500 feet under visual flight rules, the aircraft struck Mount Taranaki / Egmont about 150 feet below the summit. The 2 occupants were killed on impact and the aircraft was destroyed.
Incident date: Publish date:[A preliminary investigation showed that the circumstances were not likely to have significant implications for transport safety. Consistent with section 13 of the TAIC Act the Commission discontinued the investigation and no report was published.]
Incident date: Publish date:[A preliminary investigation showed that the circumstances were not likely to have significant implications for transport safety. Consistent with section 13 of the TAIC Act the Commission discontinued the investigation and no report was published.]
Incident date: Publish date:[A preliminary investigation showed that the circumstances were not likely to have significant implications for transport safety. Consistent with section 13 of the TAIC Act the Commission discontinued the investigation and no report was published.]
Incident date: Publish date:On Tuesday 16 November 2004, HL7597 was a Boeing 777-200, operating as flight AAR 607 on a scheduled flight from Incheon, South Korea to Auckland with 200 passengers and 17 crew on board. As AAR 607 approached Auckland runway 23L, a work party was cleared onto the closed section of the runway for further work. However, the work party were concerned about the low approach of the landing aircraft, so elected to remain clear of the runway.
Incident date: Publish date:Between Friday 5 November 2004 and Monday 21 March 2005, there were 4 freight train derailments at various locations as a result of failures of roller bearing units. These failures occurred on varying wagon classes and bogie types. There were no injuries in any of the incidents. Because of the similarities arising from each derailment, the investigations into all 4 incidents have been combined into one report. Safety issues identified included: · the reporting and tracking of component replacement
Incident date: Publish date: