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Maritime MO-2004-208

On 13 May 2004, a party of 18 passengers hired 2 jet boats to take them for a trip on Waimakariri River, north of Christchurch. At the conclusion of the trip, at about 1700, while the driver of CYS was manoeuvring back onto the boat's trailer, the reverse duct jammed in the down, or astern, position. The driver tried to rectify the problem, but the boat was caught in the swift flowing current and was swept towards a motorway bridge, less than 100 m downstream. The driver tried to manoeuvre the boat, but he was unsuccessful and it collided with one of the bridge supporting piers.

Incident date: Publish date:
Aviation AO-2004-004

[A preliminary investigation showed that the circumstances were not likely to have significant implications for transport safety. Consistent with section 13 of the TAIC Act the Commission discontinued the investigation and no report was published.]

Incident date: Publish date:
Rail RO-2004-114

[Investigation incorporated in report 04-123. Please refer to that report.]

Incident date: Publish date:
Rail RO-2004-113

On Tuesday 27 April 2004 at about 1605 hours, express freight Train 220 collided with the empty trailer of a fertiliser truck and trailer unit at a farm access level crossing between Maewa and Rangitawa on the North Island Main Trunk. The front bogie of the lead locomotive derailed and the truck and trailer unit was extensively damaged. One traction mast was knocked over and the overhead catenary brought down. The locomotive engineer and the truck driver both suffered minor injuries. The safety issues identified were: • the legal status of the level crossing

Incident date: Publish date:
Aviation AO-2004-003

On Friday 23 April 2004, Helicopter Services UH-1B helicopter ZK-HSF was on a ferry flight to Gore to facilitate maintenance work. En-route near Mokoreta a main rotor blade separated, the helicopter broke up and fell to the ground. The pilot, the sole occupant, was killed and the helicopter was destroyed. The accident resulted from fatigue failure of a tension-torsion (TT) strap, a critical rotor hub component. The fatigue cracking had probably been initiated by an unreported rotor overspeed event. Safety issues identified included:

Incident date: Publish date:
Rail RO-2004-112

On Friday, 16 April 2004, at about 1725, smoke was observed coming from beneath Train 2146 as it departed Newmarket. The train stopped at the next station, Boston Road. The passengers were evacuated and the fire was extinguished with the assistance of the New Zealand Fire Service. There were no injuries. The safety issues identified were: - the fittings connecting the oil inlet hose to the engine and the turbocharger - the shroud panels surrounding the auxiliary engine. One safety recommendation was made to the Chief Executive of Auckland Regional Transport Authority

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Maritime MO-2004-207

On Thursday 15 April 2004 at about 0215, the fishing vessel "Poseidon" grounded on a beach north of Manukau Heads while on passage from fishing grounds off Kawhia to Onehunga. The skipper was able to transmit a mayday call and the crew were winched off the vessel by rescue helicopter. On the evening of 16 April 2004 a salvage team refloated the "Poseidon". There were no injuries. The vessel suffered extensive damage to its hull and fitments. Safety issues identified included: • the lack of a watchkeeping monitor alarm for a single-handed wheelhouse operation

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Rail RO-2004-111

On Wednesday 14 April 2004, at 1504, Train 736, a Christchurch-Picton express freight service was signalled into the Christchurch-Belfast section of the Main North Line that was already occupied by a track maintenance gang. The occupation had been authorised by an outgoing train controller. Three track maintenance personnel had to take evasive action when the train passed through their worksite. There were no injuries or equipment damage. Safety issues identified included: - the lack of forward planning on the train control diagram

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Rail RO-2004-110

The Transport Accident Investigation Commission is an independent Crown entity established to determine the circumstances and causes of accidents and incidents with a view to avoiding similar occurrences in the future. Accordingly it is inappropriate that reports should be used to assign fault or blame or determine liability, since neither the investigation nor the reporting process has been undertaken for that purpose.

Incident date: Publish date:
Maritime MO-2004-206

[A preliminary investigation showed that the circumstances were not likely to have significant implications for transport safety. Consistent with section 13 of the TAIC Act the Commission discontinued the investigation and no report was published.]

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Rail RO-2004-109

On Sunday 28 March 2004, at about 1541 shortly after entering the Otira Tunnel Train 804, the Greymouth to Christchurch Tranz Alpine passenger express, with 268 passengers and 6 crew on board, stalled and slid backwards. The locomotive engineer eventually brought the train under control but when he attempted to move forward again the locomotives could not develop traction and the train stopped.

Incident date: Publish date:
Rail RO-2004-108

[A preliminary investigation showed that the circumstances were not likely to have significant implications for transport safety. Consistent with section 13 of the TAIC Act the Commission discontinued the investigation and no report was published.]

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