A pair of coupled loco-motives ran through wrongly-set points, dislodged fail-safe equipment, and carried on into a maintenance depot, shunting a maintenance vehicle into a rail wagon. There were no injuries. The wrong-routing happened because nobody checked to ensure correct setting of the points, and local procedures to prevent wrong-routing did not conform fully to KiwiRail rules. Safety actions taken by the operator precluded any need for recommendations.
Incident date: Publish date:A refuse collection truck entered a level crossing, very likely without stopping at the Stop sign, and was struck by a log train. The truck driver died in the accident. Even if the truck had stopped, the view lines weren’t good enough for the truck to clear the crossing if a train had been just out of view. Legislation is unclear on allocation of responsibility for safety of crossing users. Road users must be cautious. Wearing seatbelts will increase the chances of survival.
Incident date: Publish date:There was a fire in the cargo hold of the Kokopo Chief while berthed at the Port of Tauranga. An alarm alerted the crew to smoke in one of the cargo holds and they activated the fire extinguishing system. The main cargo on the ship was understood to have been dressed timber. Deck containers with dangerous goods were removed. There were no reported injuries. [As initially reported, subject to change, not official findings.]
Incident date: Publish date:TAIC has published its Final Report on the immobilisation and tagging of an Auckland metropolitan passenger train in September 2017. TAIC recommended that the train operator improve training for train crews, including liaising with emergency services. A fast and efficient emergency response depends on first responders receiving clear, concise and timely information.
Incident date: Publish date:An Airbus A320 inadvertently flew below minimum safe height on approach to Christchurch Airport. It landed safely. Lesson: properly used automated flight navigation systems will reduce crew workload and result in safer flight operations. Crew chose not to use auto, did not stay aware of their location compared to standard arrival route, and air traffic controller did not alert the flight crew.
Incident date: Publish date:The Australian Transport Safety Bureau has commenced an investigation and requested assistance from TAIC as an Accredited Representative in accordance with Annex 13 to the ICAO Convention. A fatal accident occurred on 16 June 2017, involving an Australian-registered Fletcher aeroplane near Bathurst, Australia. The aeroplane was manufactured in New Zealand. The aeroplane was involved in aerial agricultural operations when it collided with terrain. The pilot was fatally injured and the aeroplane destroyed. [As initially reported, subject to change, not official findings.]
Incident date: Publish date:An accredited representative has been appointed to assist the investigation of the United Arab Emirates General Civil Aviation Authority. Royal New Zealand Air Force C130 was on approach to Dubai aerodrome in instrument meteorological conditions under the control of local Air Traffic Control. The controller cleared the aeroplane to descend to 2,000 feet, which was 800 feet below the minimum radar vectoring altitude of 2,800 feet. The aeroplane had only 200 feet clearance above the highest obstacle in the area. [As initially reported, subject to change, not official findings.]
Incident date: Publish date:New Zealand has completed its support for this inquiry. Please note: TAIC will not be producing a report for this inquiry.
Incident date: Publish date:A loaded passenger train had perceived brake problems and halted soon after departure from Wellington Station. There were differences between track hardware, the signaller’s information screen, and mistaken impressions that resulted. With authorisation from the signaller, the train began to return to the station. Just then, the signaller saw that the returning train was heading into the path of an inbound train. The signaller called the driver, who stopped the train. No collision, nobody injured.
Incident date: Publish date:A BK117 helicopter was transporting a power pole. Pilot at risk of distraction, didn’t recognise and respond promptly to unanticipated yaw (helicopter unexpectedly turning about its vertical axis). The pilot lost control and ditched in shallow water. Minor injuries for pilot, substantial damage to helicopter.
Incident date: Publish date:Two broken springs in the landing gear of an ATR passenger aircraft caused it to divert and make an emergency landing. Little damage, no injuries. Springs broke when cracks formed due to corrosion. Operator found no other such problematic springs on its ATR72 fleet, has new maintenance & replacement plan. Manufacturer updated maintenance manual worldwide, added training scenario based on this incident
Incident date: Publish date:Two trains were put into conflict due to a signal box display not showing track and points layouts correctly, but a driver realised he was on wrong track and stopped his train. Safety issues related to the change management process for upgrading the signal box, and signaller familiarity with the actual track layout and equipment capabilities. Two recommendations have been made to KiwiRail, on top of safety actions taken.
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