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Aviation AO-2007-005

On 29 May 2007, a Saab SF340A aircraft that was holding on an angled taxiway at Auckland International Airport was inadvertently cleared to line up in front of a landing Raytheon 1900D. The aerodrome controller transmitted an amended clearance, but the transmission crossed with that of the Saab crew reading back the line-up clearance. The pilots of both aircraft took action to avoid a collision and stopped on the runway without any damage or injury.

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Rail RO-2007-109

[A preliminary investigation showed that the circumstances were not likely to have significant implications for transport safety. Consistent with section 13 of the TAIC Act the Commission discontinued the investigation and no report was published.]

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Rail RO-2007-108

On Saturday 12 May 2007, at 0400, northbound express freight Train 720 travelled past Seddon towards Vernon on the Main North Line without the authority of a track warrant issued from train control. The locomotive engineer did not stop on the main line at Seddon as required and obtain a new track warrant to travel beyond Seddon. Southbound Train 723 was sitting on the loop when Train 720 passed through Seddon. There were no other conflicting movements and as a result there was no damage or injury. Safety issues identified were:- • management of fatigue in train operations

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Aviation AO-2007-004

On Thursday 3 May 2007 at about 2120, ZK-NGK, an Air New Zealand Boeing 737 319, en route from Wellington to Auckland, was landed at Royal New Zealand Air Force (RNZAF) Base Ohakea as a precaution because of fumes in the cockpit from electrical burning. On board the aircraft were 121 passengers, 3 cabin crew and 2 pilots. Nobody was injured in the incident.

Incident date: Publish date:
Rail RO-2007-107

[A preliminary investigation showed that the circumstances were not likely to have significant implications for transport safety. Consistent with section 13 of the TAIC Act the Commission discontinued the investigation and no report was published.]

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Maritime MO-2007-206

On Saturday 14 April 2007 at about 0300, the tug Nautilus III was towing the barge Kimihia, which was loaded with a cargo of rock, through the Wellington Harbour entrance channel when the barge unexpectedly capsized and deposited its cargo onto the seabed of the main entrance channel to the port. The master and crew of the tug, after advising Wellington Harbour Radio of the accident, towed the barge in its inverted state to Miramar wharf where salvage experts were able to right the barge on the 18 April 2007. Safety issues identified included:

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Rail RO-2007-106

[A preliminary investigation showed that the circumstances were not likely to have significant implications for transport safety. Consistent with section 13 of the TAIC Act the Commission discontinued the investigation and no report was published.]

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Rail RO-2007-105

Between June 2006 and April 2007 the Transport Accident Investigation Commission (the Commission) launched inquiries into 5 separate platform overrun events on the Auckland suburban rail network. Because there appeared to be a number of common factors contributing to the overruns, they have been combined into this one report.

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Aviation AO-2007-003

On Thursday 5 April 2007, ZK-DOJ, a Piper PA32S-300 Cherokee 6, was on a local charter flight from Queenstown with a pilot and 2 passengers on board. The flight was to include a landing and short stopover at Elfin Bay on the shores of Lake Wakatipu, before returning to Queenstown. During the landing at Elfin Bay, the pilot deliberately steered the aircraft off the side of the airstrip to avoid overrunning the end. The aircraft struck a fence and sustained moderate damage but there was no injury to the passengers or pilot.

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Rail RO-2007-104

[A preliminary investigation showed that the circumstances were not likely to have significant implications for transport safety. Consistent with section 13 of the TAIC Act the Commission discontinued the investigation and no report was published.]

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Aviation AO-2007-002

On Friday 30 March 2007, Dornier 228-202 ZK-VIR was on a positioning flight from Westport to Christchurch, when the 2-pilot crew became light-headed and felt faint. Concerned about their safety, the crew was able to descend the aircraft and make a safe landing at Christchurch. They subsequently made a full recovery. No cause for the effects felt by the crew could be identified. The aircraft eventually entered revenue service and no further incidents were reported.

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Aviation AO-2007-001

On Thursday 22 March 2007 at 1615, A6 EBC, an Emirates Boeing 777-300ER, with 357 passengers, 16 cabin crew and 2 pilots on board, started its take off on runway 05 Right at Auckland International Airport bound for Sydney.

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