On Saturday 19 May 2001, at 1450, Boeing 767-319 ZK-NCH was on approach to land at Auckland International Aerodrome when a section of a wing flap deflection control track separated from the aeroplane. The 3 kg section penetrated the roof of an occupied warehouse and fell to the floor without causing personal injury. The crew of ZK-NCH were unaware of the event and continued with a successful landing.
Incident date: Publish date:On Monday 14 May 2001, the passenger charter vessel, "Osprey", with the skipper and 6 passengers on board, departed Tolaga Bay for a half-day fishing trip. At about 0830, while crossing the Uawa River bar outbound, the boat encountered 2 waves substantially larger than those already crossed. The first wave heeled the boat significantly to port, causing all on board to lose their footing. One passenger was thrown overboard. The second wave passed over the boat and caused substantial damage to the boat and flooding of the cockpit.
Incident date: Publish date:On Sunday 6 May 2001, at about 0838, a collision occurred between express passenger Train 600, Bay Express, and an excavator and front end loader working on the up main line at Muri, 31.4 km North Island Main Trunk. The maintenance plant was operating under Conditional Stop Protection when the collision occurred. Train 600 had been given authority to pass through the protected site at a time when one of the four work groups operating within an 11.9 km protected length understood they were clear to work. There were no injuries.
Incident date: Publish date:[A preliminary investigation showed that the circumstances were not likely to have significant implications for transport safety. Consistent with section 13 of the TAIC Act the Commission discontinued the investigation and no report was published.]
Incident date: Publish date:On Sunday 15 April 2001, at about 2327, the liquefied petroleum gas carrier "Boral Gas" was outbound from the terminal in Papakura Channel in Manukau Harbour with 14 crew and a licensed harbour pilot on board when it grounded in soft mud on the north side of the channel. After nearly 2 hours the ship was refloated and continued its passage. There were no injuries and the ship suffered no structural damage. The grounding resulted from the pilot losing situational awareness primarily due to 4 consecutive light beacons marking the channel being extinguished.
Incident date: Publish date:On Friday 23 March 2001, at 0705, Hughes 369D helicopter ZK-HMN experienced an engine flameout as the pilot applied collective control normally to arrest the helicopter’s descent. The pilot landed the helicopter in trees on a mountain slope at about 3000 feet, some 12 km northwest of Milford Sound. The pilot and the crew member on board the helicopter were uninjured.
Incident date: Publish date:On Thursday 15 March 2001, at about 0517, the coastal container ship "Spirit of Enterprise" was outbound from Dunedin in Otago Harbour with 11 crew on board under the control of its pilot exempt master, when it sheered violently to port turning through 180 degrees in the channel at Deborah Bend. The master took the ship back to the swinging basin off Port Chalmers where tests of the steering machinery were carried out. Finding no faults, the master resumed the outward passage but again the vessel sheered at Deborah Bend, this time touching the channel side.
Incident date: Publish date:On Friday, 9 March 2001 at 0922, ZK-RCA, a Fairchild SA227-AC Metro III operating as NZ 2703 from Auckland, struck a flock of birds on landing at Tauranga Aerodrome. During the ground roll the left-hand engine failed and the aircraft was brought to a halt to complete the engine shutdown checklist. While taxiing to the terminal the right-hand engine spooled down. The 16 passengers were disembarked and the aircraft was towed to the terminal. ZK-RCA’s left-hand engine was replaced and the aircraft returned to service after 3 days. There were no injuries.
Incident date: Publish date:On Friday 9 March 2001, at about 0725, the tug "Nautilus III" was towing the laden hopper barge H7 in Auckland Harbour when the barge took a sheer to starboard. The tug skipper manoeuvred the tug in an attempt to arrest the sheer but the tug was girted, capsized, and sank. The skipper of the tug swam clear and was not injured. The main factors contributing to the accident were the short length of the towline in use, the set-up of the towline and the compromise of the watertight integrity of the tug. Safety issues identified included:
Incident date: Publish date:On Wednesday 7 March 2001 at about 2233 Train 531, a southbound express freight train collided with the rear of Train 547, another southbound express freight service which had stalled on the Mokoia Bank between Whareroa and Mokoia on the Marton to New Plymouth Line. Train 531 had entered the section and was going to assist Train 547 when the collision occurred. The locomotive engineer of Train 547 had not protected the rear of his disabled train to warn the locomotive engineer of Train 531 as he approached. Safety issues identified included:
Incident date: Publish date:This report examines 6 track heat buckle incidents that occurred in different localities throughout New Zealand in the summer of 2000/2001, 5 of which resulted in derailments. Safety issues identified by these incidents included: • the need for training of track staff to ensure they recognise and respond to visible track defects • the possible need to protect continuous welded rail, formed at an unknown neutral temperature, during hot weather • the need to control tamping and lining to ensure track is not realigned leaving increased compressive stress in the rails
Incident date: Publish date:[A preliminary investigation showed that the circumstances were not likely to have significant implications for transport safety. Consistent with section 13 of the TAIC Act the Commission discontinued the investigation and no report was published.]
Incident date: Publish date: