On 16 October 1993, MIL MI-8T helicopter YS-1005P, went out of control and broke up while in cruise flight. An uncommanded yaw led to a pitch excursion severe enough for the main rotor to strike and sever the tail boom. The helicopter's three occupants were killed in the accident. The precise cause of the uncommanded yaw could not be determined.
Incident date: Publish date:At 1030 hours on Thursday 2 May 1996, two Hi-Rail vehicles collided on a curve near Kotemaori on the Palmerston North-Gisborne Line. The four occupants of the vehicles were uninjured. The cause of the collision was insufficient information available to the employee in charge of one of the Hi-Rail vehicles.
Incident date: Publish date:The aircraft departed from New Plymouth to Hamilton at 1752 hours. Nothing was heard from the aircraft after the pilot acknowledged his take-off clearance. A search aircraft located the pilot's body off the coast of Urenui next day. The aircraft was not found.
Incident date: Publish date:TAIC report: people in control of transport infrastructure need to think again about how well their structures can cope with climate change significant rainfall events. Flood water washed out rail track ballast. Freight train ran over the track. Locomotive and 17 of its 37 wagons derailed. KiwiRail has addressed safety issues with severe weather warning, flood monitoring
Incident date: Publish date:At about 2125 hours on Friday 4 December 1998, a loss of separation occurred between an Air New Zealand Boeing 767 and a Sunair Piper Aztec near Auckland Airport. Both aircraft were under radar control at the time of the incident. The Boeing 767, on departure from Auckland, was intercepting the Auckland - Rarotonga track and climbing to flight level 250. The Piper Aztec was en route from Hamilton to Whangarei via Auckland, maintaining 7000 feet. The pilot of the Piper Aztec saw the Boeing 767 closing from the left and descended to ensure separation.
Incident date: Publish date:At 1105 hours on Tuesday 17 December 1996, Air New Zealand flight NZ 31 from Auckland to Brisbane, requested a clearance to climb from flight level 350 to non-standard flight level 370, because of turbulence at flight level 350. The level change was authorised by air traffic control, and as the aircraft left flight level 350, the crew noticed the "contrails" of another aircraft above and levelled off. A traffic alert and collision avoidance system traffic advisory message was received at the same time, indicating that the vertical separation of the aircraft on passing was 1800 feet.
Incident date: Publish date:At about 1225 hours on 29 March 1995, ZK-TIK stalled and spun from a low altitude after having both engines fail within a short space of time. The aeroplane had just departed Hamilton on a scheduled flight to New Plymouth. All six occupants died in the accident. Causal factors identified were a fuel tank mis-selection and failure to execute a forced landing. A contributing factor was a fuel management regime with potential for mismanagement. Safety issues discussed are checks and communications in emergency.
Incident date: Publish date:The Commission is investigating a runway incursion incident at Hamilton Aerodrome involving an Airbus A320 aeroplane registration VH-A5E operating as JQ166 operated by Jetstar Airways and a Cessna 172 registration ZK-TAP operated by Ardmore Flying School. The reported circumstances were that the A320 was on the ground, backtracking along the aerodrome’s main runway 18L ahead of departing for Sydney. The Cessna was airborne, approaching to land; on the same runway.
Incident date: Publish date: Not yet publishedTAIC final report shows why equipment should be operated by people who understand how to use it safely, and why safety management systems should require ongoing monitoring and review of risk control effectiveness. A container ship crew member's leg was seriously injured when caught in a moving part of a telescopic ladder.
Incident date: Publish date:KiwiRail’s system for work in the rail corridor should satisfy the needs of the contractors as well as KiwiRail, and it should not deter contractors from applying to enter the rail corridor. A fatal accident where a train impacted a road contractor’s truck on a level crossing happened because KiwiRail was unaware the road-marking crew would be there; they had not applied for a permit to work in the rail corridor.
Incident date: Publish date:On Monday, 27 November 1995 at approximately 1600 hours, during a summer white water rafting trip down the Shotover River near Queenstown a raft capsized and one of the passengers drowned. Safety issues identified included the difficulty rafting operators have in conveying the nature of white water rafting to non-English speaking passengers. It was recommended that the proposed Commercial White Water Rafting Code of Practice include a requirement for raft operators to show passengers an audio-visual summary of the demands of the rafting experience before they embark on the trip.
Incident date: Publish date:On Tuesday, 25 July 1995 an accident occurred during a winter white water rafting trip down the Shotover River, Queenstown. The raft failed to follow the intended passage down the Cascade Rapid and was drawn sideways into a rapid/waterfall known as The Toaster. One of the passengers fell from the raft, became entrapped underwater and drowned. Safety issues identified included levels and methods of training for rafting guides. The Safety issues identified are being addressed by the Maritime Safety Authority by way of the Draft Code of Practice for Raft Operators.
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