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Rail RO-1998-106

On Saturday 28 March 1998 at 1707 hours Train 201, the southbound Auckland to Wellington Overlander passenger express, struck a displaced load on Train 242, a Wellington to Palmerston North express freight train which was berthed in the Longburn loop. There were no injuries. Train 201 suffered superficial damage to the locomotive and carriages. Safety deficiencies identified were: · the lack of appreciation of correct load securing requirements · insufficient training of staff involved in loading

Incident date: Publish date:
Maritime MO-1998-205

At about 1050 on Monday, 23 March 1998, a commercial jet boat carrying 14 passengers was transiting down the upper Dart River. While negotiating a right hand bend in the river, the driver reduced power as he turned the boat hard left around a rock in midstream. When he re-applied power the engine stalled. Without directional control the driver was unable to prevent the boat striking a large rock on the river bank. The passengers and the driver received minor to serious injuries in the accident. Seven passengers were evacuated by helicopter.

Incident date: Publish date:
Maritime MO-1998-204

At about 0826 on Monday, 16 March 1998, "Condor 10" was proceeding out of Wellington Harbour into a moderate southerly swell, when the vessel encountered two short steep waves of approximately 4.5 m in height. The master reduced speed as "Condor 10" rose over the first wave, and the vessel dipped onto the face of the second wave. The resultant slamming displaced the bow visor and caused substantial damage to the surrounding hull structure. None of the 231 passengers and 22 crew were injured in the incident. Safety issues identified included:

Incident date: Publish date:
Rail RO-1998-105

On Saturday, 14 March 1998, at about 1802 hours a displaced stack of platform containers on Train 235, a Westfield to Wellington express freight train, struck a through-truss bridge at Ngaruawahia. As a result of the collision the train parted, six wagons were derailed, and major damage to the bridge occurred when five wagons and various loads concertinaed. The cause of the collision was the movement of inadequately restrained stacked platform containers. Safety issues identified were: • the serviceability and uniformity of integral interlocking devices fitted to platform containers;

Incident date: Publish date:
Aviation AO-1998-003

[A preliminary investigation showed that the circumstances were not likely to have significant implications for transport safety. Consistent with section 13 of the TAIC Act the Commission discontinued the investigation and no report was published.]

Incident date: Publish date:
Rail RO-1998-103

On Monday, 9 March 1998, at about 0655 hours Train 1603, a Masterton to Wellington suburban passenger service, collided with a transition head which had fallen from the locomotive cowcatcher. Damage to the underside of the train resulted in a 3000 litre diesel fuel spillage. The cause of the collision was a transition head becoming displaced in transit due to inadequate stowage details. Safety deficiencies identified were: • The lack of adequate investigation of the work necessary to convert overseas rolling stock for New Zealand coupling requirements.

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Rail RO-1998-104

On Monday 9 March 1998 at about 2359 hours, nine wagons of Train 928, a northbound Dunedin to Christchurch express freight, derailed near Purakanui at low speed. The train continued for approximately four kilometres before a brake application alerted the locomotive engineer to the problem. The point of the derailment coincided with that of an almost identical derailment involving Train 928 on 3 March 1998.

Incident date: Publish date:
Aviation AO-1998-004

[A preliminary investigation showed that the circumstances were not likely to have significant implications for transport safety. Consistent with section 13 of the TAIC Act the Commission discontinued the investigation and no report was published.]

Incident date: Publish date:
Maritime MO-1998-203

[A preliminary investigation showed that the circumstances were not likely to have significant implications for transport safety. Consistent with section 13 of the TAIC Act the Commission discontinued the investigation and no report was published.]

Incident date: Publish date:
Maritime MO-1998-202

At about 0810 on Friday, 6 March 1998, the harbour tug "Purau" and the Diamond Harbour ferry Ngatiki, with eight passengers on board, were in collision in the Port of Lyttelton. The ferry was severely damaged and all except one passenger received minor injuries.

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Rail RO-1998-102

On Monday, 16 February 1998 at approximately 1630 hours, Train 924, a northbound Invercargill to Dunedin express freight was travelling at the maximum allowable line speed of 80 km/h when the locomotive engineer noticed a minor alignment ripple in the track ahead. The locomotive negotiated this area with only a slight lurch but 14 of the wagons in the body of the train became derailed as they traversed the misalignment.

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Rail RO-1998-101

On Thursday, 5 February 1998 at about 1630 hours, Train 721, a southbound Picton to Christchurch express freight was near Scargill when the locomotive engineer noticed a buckle in the track ahead. He was unable to slow the train significantly in the limited distance available and although the locomotive and the three leading wagons traversed the buckled track, the following eleven wagons became derailed before the train came to a stop. A safety issue identified was the failure of the safety system to achieve adequate protection of a predictable weak spot.

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