The Marine Accident Investigation Branch investigated this ocurrence on behalf of TAIC, and published their findings as which can be found using the link in the sidebar to the right.
Incident date: Publish date:On Wednesday 26 May 1999, at approximately 0730 hours, a rake of empty log wagons was being propelled from the Kinleith railway yard into Carter Holt Harvey Limited's siding when the leading wagon hit the "bull-bars" of a logging truck parked foul of the running road. The remote control operator who was on the leading wagon jumped clear just prior to the collision but stumbled and fell against the wagon and was dragged for approximately 10 m before rolling clear. He received broken ribs and abrasions as a result of the accident.
Incident date: Publish date:The Commission assisted the Aircraft Accident Investigation Bureau of Switzerland in their investigation of this accident. The Swiss report was released 28 September 2011 and is available (in French only) on the Bureau's website using the link in the sidebar to the right. The accident was a collision with terrain after the flight, conducted under visual flight rules, was continued into instrument meteorological conditions.
Incident date: Publish date:On Thursday 3 April 1997, at 1912 hours, the Airways Corporation communications network system suffered a failure which caused a temporary loss of all Air Traffic Control very high frequency radio communications in the Wellington Sector. Subsequent modifications to the system and procedures will reduce the chance of a similar failure. A safety issue identified was the inadequacy of the "communications failure" information in the Instrument Flight Guide for pilots, in the case of a failure of communications from Air Traffic Control.
Incident date: Publish date:On Wednesday, 13 August 2008 at 0941, express freight Train 845, a westbound Lyttelton to Ngakawau empty coal service, overran its track warrant limit at Reefton. The locomotive engineer continued to drive the train for a further 8.75 kilometres before he realised what had happened and stopped the train. There were no conflicting movements or track engineering occupations.
Incident date: Publish date:[A preliminary investigation showed that the circumstances were not likely to have significant implications for transport safety. Consistent with section 13 of the TAIC Act the Commission discontinued the investigation and no report was published.]
Incident date: Publish date:On Thursday 12 May 2005, at about 0410, Train 211, a southbound express freight service, passed signal 8L at the north end of Rangitawa at Stop. The train continued on the main line until the locomotive engineer regained situational awareness and stopped the train. Train 230, a northbound express freight train, was approaching Rangitawa from the south end and had been signalled to enter the loop at the time. When Train 211 passed Signal 8L at Stop, the signal governing the entry of Train 230 into the loop reverted to Stop and Train 230 stopped about 100 m short of the signal.
Incident date: Publish date:On 6 April 2012 the 9.5-tonne body of a damaged freight wagon (the load) was being carried on a purpose-built "special-movement wagon" (the wagon). The wagon was one of 60 on a northbound freight train travelling from Dunedin to Christchurch.
Incident date: Publish date:Bantam B22 microlight aircraft ZK-JAS underwent an uncontrolled descent and collision with the ground near the Rotorua Microlight Club airstrip at Mead Road, near Rotorua, on 12 December 1993. Safety issues included the hazard of reduced performance due to excess load, high density altitude, and sink encountered after take-off, and potential for stall onset during a turn at low airspeed.
Incident date: Publish date:At about 0615 on Thursday, 13 September 2001, an unattached loaded log wagon on the leading end of a shunt being propelled into a siding at Stillwater was routed onto the main line at a damaged turnout and rolled 450 m downgrade on the Midland Line. Thick fog was present at the time and the loss of the wagon was not realised until 0645 and it was not located until 0700. The safety issues identified included: • rail service operations being carried out by non-qualified contractors at Stillwater
Incident date: Publish date:Between June 2006 and April 2007 the Transport Accident Investigation Commission (the Commission) launched inquiries into 5 separate platform overrun events on the Auckland suburban rail network. Because there appeared to be a number of common factors contributing to the overruns, they have been combined into this one report.
Incident date: Publish date:On Wednesday 7 August 2002, at about 1335, train control gave authority for westbound express freight Train 484 to depart Tauranga and enter a section of track already occupied by a hi-rail vehicle travelling towards the train. Some minutes after the train departed, the train controller in-training realised he had set up a potential collision so he contacted the locomotive engineer and instructed him to stop the train. When the train stopped, about 300 m separated the train and the hi-rail vehicle. The safety issues identified included:
Incident date: Publish date: