At about 0400 on 19 November 2000, the Auckland Harbour tug "Waka Kume", with 2 crew aboard, was made fast to the port quarter of a ship berthing at the Fergusson Container Terminal. As the ship was moving astern towards the berth the pilot decided to abort the approach due to the bow thruster on the ship not being able to hold the bow up into the wind and tide.
Incident date: Publish date:[A preliminary investigation showed that the circumstances were not likely to have significant implications for transport safety. Consistent with section 13 of the TAIC Act the Commission discontinued the investigation and no report was published.]
Incident date: Publish date:On Friday 17 November 2000 at about 1840, the fishing charter vessel "La Nina", with 9 passengers and 2 crew on board, was on passage to an anchorage in a bay on Rakitu Island when it grounded on rocks to the north-east of the island. The passengers and crew boarded a liferaft shortly before the vessel foundered. They were later rescued by other vessels, which had answered the Mayday call sent by the skipper. The deckhand was seriously injured during the grounding. Safety issues identified included: • inadequate safety briefing before commencing charter
Incident date: Publish date:On Saturday 28 October 2000, Balloons over Taupo Cameron A-180 hot air balloon ZK-FAS was on a local flight near Taupo with 7 passengers and one crew when an unanticipated wind increase necessitated a prompt landing. During the landing approach the pilot endeavoured to extend the flight path over a power line which he had seen at a late stage. The balloon basket struck and broke the 3 wires of the power line before landing in the next paddock. There were no injuries and no damage to the balloon.
Incident date: Publish date:[A preliminary investigation showed that the circumstances were not likely to have significant implications for transport safety. Consistent with section 13 of the TAIC Act the Commission discontinued the investigation and no report was published.]
Incident date: Publish date:On Wednesday 25 October 2000 at 1936, the Christchurch main trunk air traffic services centre communications system experienced an unanticipated complete power loss during non routine maintenance. The power loss caused a loss of normal radio and telephone communications to the centre for several minutes. Each terminal controller and the controllers for 2 of the 5 area sectors had independent battery powered radios available. Independent telephone links and all radar information to the centre remained operational.
Incident date: Publish date:On Tuesday 17 October 2000, at about 1250, a MDHC 369E helicopter ZK-HFT, was returning to Queenstown with 2 people on board when the pilot made a forced landing owing to a loss of engine power.
Incident date: Publish date:On Wednesday, 4 October 2000, Train 225, an Auckland to Wellington express freight service, was permitted to depart from Te Kauwhata on the North Island Main Trunk and enter the down main line that was already occupied by an authorised hi-rail vehicle movement. No collision resulted, as the four occupants of the hi-rail vehicle became aware of Train 225’s approach and were able to off-track before the train passed. The safety issues identified included: • a train controller not following procedures for handling track user inquiries
Incident date: Publish date:On Friday 22 September 2000, at about 2338, express freight Train 521 derailed when travelling too fast for the first curve encountered descending the 1 in 35 down grade on the Westmere bank. The 2 locomotives were severely damaged when they overturned following the derailment. The locomotive engineer received only minor injuries. The reason for the excessive speed was the locomotive engineer’s loss of awareness during a microsleep.
Incident date: Publish date:At about 1640 on Tuesday 19 September 2000, Train P28 Pahiatua - Palmerston North shunting service passed signal 4R at Danger and entered the main line at Woodville which was occupied by opposing Train 601 Bay Express passenger express. Train 601 had a Clear Proceed signalled route and was not expecting to stop. The conflict was soon realised and both trains were brought to a stop about 750 m apart. Train P28 derailed when its locomotive engineer tried to reverse off the main line through a set of points that had been "run through" when the signal had been passed at Danger.
Incident date: Publish date:On Saturday 22 July 2000, at about 1927, express freight Train 378 derailed when it entered a crossover at the north end of Te Maunga while travelling too fast. The locomotive was severely damaged when it overturned following the derailment. The locomotive engineer suffered minor injuries. The train controller had incorrectly set a medium speed route to Mount Maunganui instead of the intended high speed route to Tauranga. The locomotive engineer did not react to the unexpected signal aspects displayed. Safety issues identified included:
Incident date: Publish date:[A preliminary investigation showed that the circumstances were not likely to have significant implications for transport safety. Consistent with section 13 of the TAIC Act the Commission discontinued the investigation and no report was published.]
Incident date: Publish date: