Skip to main content

Inquiries & Recommendations
Ngā ketuketutanga me ngā tūtohunga

Search Results

445-456 of 1161 results
Aviation AO-2002-002

On Friday, 25 January 2002, at about 1430, Piper PA34-200T Seneca ZK-SFC was on approach to land at Gisborne Aerodrome when the nose undercarriage failed to extend. After several unsuccessful attempts to extend the nose undercarriage, the pilot diverted to Hastings Aerodrome where a full wheels-up landing was completed. The 2 crew members and one passenger on board were uninjured and the aircraft sustained minor damage.

Incident date: Publish date:
Rail RO-1999-103

On Wednesday 11 March 1999, at approximately 1120 hours, a head-on collision occurred between the middle ferry shunt and the siding shunt at Wellington ferry terminal. The locomotive engineer's seat in the siding shunt locomotive was torn from its mountings, and the locomotive engineer was propelled to the front of the cab, sustaining lacerations and concussion. Two shunters riding on the leading ends of their respective shunts were able to jump clear before the collision. The safety deficiencies identified included:

Incident date: Publish date:
Rail RO-1995-102

[A preliminary investigation showed that the circumstances were not likely to have significant implications for transport safety. Consistent with section 13 of the TAIC Act the Commission discontinued the investigation and no report was published.]

Incident date: Publish date:
Rail RO-2006-109

[A preliminary investigation showed that the circumstances were not likely to have significant implications for transport safety. Consistent with section 13 of the TAIC Act the Commission discontinued the investigation and no report was published.]

Incident date: Publish date:
Aviation AO-2025-004

The Commission is investigating an incident involving a Boeing 787-9 operating as NZ175 from Auckland to Perth, in international airspace over the Tasman Sea.

Incident date: Publish date: Not yet published
Maritime MO-2000-205

At about 0914 on Wednesday, 31 May 2000, the passenger ferries "Quickcat" and "Quickcat II" were operating on the ferry service between Waiheke Island and Auckland when they collided about 0.5 miles east of the northern leading light in Auckland Harbour. The visibility in the area at the time of the collision was about 50 m due to fog. There was a total of 127 passengers and 7 crew aboard the 2 vessels, none of whom were injured. Safety issues identified included: • the speed of the 2 vessels in restricted visibility • the inefficient use of radar for collision avoidance

Incident date: Publish date:
Rail RO-2004-105

[A preliminary investigation showed that the circumstances were not likely to have significant implications for transport safety. Consistent with section 13 of the TAIC Act the Commission discontinued the investigation and no report was published.]

Incident date: Publish date:
Aviation AO-1994-015

[Investigated on behalf of the Government of Fiji. Direct any inquiries for copy of the report to the Minister of Transport of that State]

Incident date: Publish date:
Rail RO-2005-115

On Friday 1 April 2005, Train 2100 was a scheduled empty passenger service being positioned to Waitakere to start passenger operations for the day. At 0627, soon after the train had passed through Ranui station, the coupling between the locomotive and the guard’s van parted. As a result of the parting, the automatic brake system lost all air pressure and brought the train to a stop.

Incident date: Publish date:
Rail RO-1998-110

On Sunday 28 June 1998, at approximately 1650 hours, Train 902, the northbound Southerner express passenger, derailed at Islington at slow speed. The rear of the train was routed to the down main when motorised points moved under the train. There were no injuries. Causal factors were non-compliances with intended procedures for points operation. Safety issues identified were the suitability of those procedures and the effectiveness of compliance monitoring. A number of safety actions were taken by the operator and 5 safety recommendations were made to address the safety issues.

Incident date: Publish date:
Rail RO-2002-113

On Thursday 25 April 2002 at about 1242 hours, a near collision occurred between passenger express Train 700 TranzCoastal and an empty petrol tanker, at Vickerman Street level crossing, near Blenheim. As the train approached the level crossing, the locomotive engineer saw the tanker obstructing the crossing and immediately sounded the horn and applied the emergency brakes. The train stopped about 5 m short of the crossing, by which time the tanker had reversed clear. There were no injuries.

Incident date: Publish date:
Aviation AO-2013-001

Please see TSB website for the full report using the link in the sidebar to the right.

Incident date: Publish date: