On Friday 23 April 2004, Helicopter Services UH-1B helicopter ZK-HSF was on a ferry flight to Gore to facilitate maintenance work. En-route near Mokoreta a main rotor blade separated, the helicopter broke up and fell to the ground. The pilot, the sole occupant, was killed and the helicopter was destroyed. The accident resulted from fatigue failure of a tension-torsion (TT) strap, a critical rotor hub component. The fatigue cracking had probably been initiated by an unreported rotor overspeed event. Safety issues identified included:
Incident date: Publish date:On Friday, 16 April 2004, at about 1725, smoke was observed coming from beneath Train 2146 as it departed Newmarket. The train stopped at the next station, Boston Road. The passengers were evacuated and the fire was extinguished with the assistance of the New Zealand Fire Service. There were no injuries. The safety issues identified were: - the fittings connecting the oil inlet hose to the engine and the turbocharger - the shroud panels surrounding the auxiliary engine. One safety recommendation was made to the Chief Executive of Auckland Regional Transport Authority
Incident date: Publish date:On Thursday 15 April 2004 at about 0215, the fishing vessel "Poseidon" grounded on a beach north of Manukau Heads while on passage from fishing grounds off Kawhia to Onehunga. The skipper was able to transmit a mayday call and the crew were winched off the vessel by rescue helicopter. On the evening of 16 April 2004 a salvage team refloated the "Poseidon". There were no injuries. The vessel suffered extensive damage to its hull and fitments. Safety issues identified included: • the lack of a watchkeeping monitor alarm for a single-handed wheelhouse operation
Incident date: Publish date:On Wednesday 14 April 2004, at 1504, Train 736, a Christchurch-Picton express freight service was signalled into the Christchurch-Belfast section of the Main North Line that was already occupied by a track maintenance gang. The occupation had been authorised by an outgoing train controller. Three track maintenance personnel had to take evasive action when the train passed through their worksite. There were no injuries or equipment damage. Safety issues identified included: - the lack of forward planning on the train control diagram
Incident date: Publish date:The Transport Accident Investigation Commission is an independent Crown entity established to determine the circumstances and causes of accidents and incidents with a view to avoiding similar occurrences in the future. Accordingly it is inappropriate that reports should be used to assign fault or blame or determine liability, since neither the investigation nor the reporting process has been undertaken for that purpose.
Incident date: Publish date:[A preliminary investigation showed that the circumstances were not likely to have significant implications for transport safety. Consistent with section 13 of the TAIC Act the Commission discontinued the investigation and no report was published.]
Incident date: Publish date:On Sunday 28 March 2004, at about 1541 shortly after entering the Otira Tunnel Train 804, the Greymouth to Christchurch Tranz Alpine passenger express, with 268 passengers and 6 crew on board, stalled and slid backwards. The locomotive engineer eventually brought the train under control but when he attempted to move forward again the locomotives could not develop traction and the train stopped.
Incident date: Publish date:[A preliminary investigation showed that the circumstances were not likely to have significant implications for transport safety. Consistent with section 13 of the TAIC Act the Commission discontinued the investigation and no report was published.]
Incident date: Publish date:On Friday 26 March 2004 at about 0215, the fishing boat "Bronny G" grounded on rocks at Steep Head on the Banks Peninsula while on passage from fishing grounds to Lyttelton Harbour. Before abandoning the boat the skipper was unable to transmit a mayday call but was able to use his cellphone to contact his partner ashore, who raised the alarm.
Incident date: Publish date:On Wednesday 24 March 2004, at about 0149, USQ 7663, the 27th wagon on southbound express freight Train 237, derailed while negotiating a left-hand curve between Puketutu and Kopaki on the North Island Main Trunk. The wagon ran derailed for about 750 m until it struck the spreader bar on the north-end facing points at Kopaki, derailing the following 4 wagons and parting the train between the 29th and 30th wagons. The condition of the trailing bogie of wagon USQ 7663 was a significant contributing factor to the derailment. Safety issues included:
Incident date: Publish date:[Assisted overseas investigation - no TAIC report published.]
Incident date: Publish date:[A preliminary investigation showed that the circumstances were not likely to have significant implications for transport safety. Consistent with section 13 of the TAIC Act the Commission discontinued the investigation and no report was published.]
Incident date: Publish date: